We pilots tend to overestimate our abilities whether we know it or not, that is part of the pilot psyche, I think. From the newly minted CFI who thinks strapping into a jet fighter is no big deal to the young airline first officer who sees no difference between what he or she is doing for a living than the "old man" in the left seat. But for all of us, at some point we have to admit that the next step is "too much airplane."

— James Albright

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Updated:

2019-10-31

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PC-12 N950KA accident wreckage,
right quartering view, NSTB

I know a Pilatus PC-12 flight instructor who flew with the pilot at the controls of this airplane on the day it broke apart at altitude. He flew with the pilot a few months before the accident on a pre-buy inspection of another PC-12. He tells me this buyer was behind the airplane from the first moment they started it and never caught up. He told the pilot he should consider always flying with a qualified instructor until he gained more experience. Needless to say, that deal fell through. But the pilot eventually bought a PC-12 and ignored the advice to hire a qualified instructor. The NTSB report not only gives a description of what happened, but also a good hypothesis about why.

1 — Accident report

2 — Narrative

3 — Analysis

4 — Cause

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1

Accident report

  • Date: 7 Jun 2012
  • Time: 1235
  • Type: Pilatus PC-12
  • Operator: Roadside Ventures, LLC
  • Registration: N950KA
  • Fatalities: 1 of 1 crew, 5 of 5 passengers
  • Aircraft fate: Destroyed
  • Phase: En route
  • Airport (departure): Fort Pierce, FL (FPR)
  • Airport (arrival): Junction City, KS (3JC)

2

Narrative

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PC-12 N950KA accident wreckage, right quartering view, NSTB

  • On June 7, 2012, about 1235 eastern daylight time, a Pilatus PC-12/47, N950KA, registered to and operated by Roadside Ventures, LLC, departed controlled flight followed by subsequent in-flight breakup near Lake Wales, Florida. Instrument meteorological conditions prevailed at the altitude and location of the departure from controlled flight and an instrument flight rules (IFR) flight plan was filed for the 14 Code of Federal Regulations (CFR) Part 91 personal flight from St Lucie County International Airport (FPR), Fort Pierce, Florida, to Freeman Field Airport (3JC), Junction City, Kansas. The airplane was substantially damaged and the private pilot and five passengers were fatally injured. The flight originated from FPR about 1205.
  • About 6 minutes after takeoff the pilot was advised by the Miami ARTCC Stoop Sector radar controller of an area of moderate to heavy precipitation twelve to two o'clock 15 miles ahead of the airplane's position; the returns were reported to be 30 miles in diameter. The pilot asked the controller if he needed to circumnavigate the weather, to which the controller replied that deviations north of course were approved and when able to proceed direct LAL, which he acknowledged. A trainee controller and a controller providing oversight discussed off frequency that deviation to the south would be better. The controller then questioned the pilot about his route, to which he replied, and the controller then advised the pilot that deviations south of course were approved, which he acknowledged. The flight continued in generally a west-northwesterly direction, or about 290 degrees, and at 1230:11, while at flight level (FL) 235, the controller cleared the flight to FL260, which the pilot acknowledged. At 1232:26, the aircraft's central advisory and warning system (CAWS) recorded that the pusher system went into "ice mode" indicating the pilot had selected the propeller heat on and inertial separator open. At that time the aircraft's engine information system (EIS) recorded the airplane at 24,668 feet pressure altitude, 110 knots indicated airspeed (KIAS), and an outside air temperature of minus 11 degrees Celsius.
  • At 1232:36, the Miami ARTCC Avon Sector radar controller advised the pilot of a large area of precipitation northwest of Lakeland, with moderate, heavy and extreme echoes in the northwest, and asked him to look at it and to advise what direction he needed to deviate, then suggested deviation right of course until north of the adverse weather. The pilot responded that he agreed, and the controller asked the pilot what heading from his position would keep the airplane clear, to which he responded at 1233:04 with, 320 degrees.
  • At 1233:08, the Miami ARTCC Avon Sector radar controller cleared the pilot to fly heading 320 degrees or to deviate right of course when necessary, and when able proceed direct to Seminole, which he acknowledged at 1233:16. There was no further recorded communication from the pilot with the Miami ARTCC.
  • Radar data showed that between 1233:08, and 1233:26, the airplane flew on a heading of approximately 290 degrees, and climbed from FL250 to FL251, while the EIS recorded for the same time the airplane was at either 109 or 110 KIAS and the outside air temperature was minus 12 degrees Celsius. The radar data indicated that between 1233:26 and 1233:31, the airplane climbed to FL252 (highest recorded altitude from secondary radar returns). At 1233:30, while at slightly less than 25 degrees of right bank based on the NTSB Radar Performance Study based on the radar returns, 109 KIAS, 25,188 feet and total air temperature of minus 12 degrees Celsius based on the data downloaded from the CAWS, autopilot disengagement occurred. This was recorded on the CAWS 3 seconds later. The NTSB Performance Study also indicates that based on radar returns between 1233:30, and 1233:40, the bank angle increased from less than approximately 25 degrees to 50 degrees, while the radar data for the approximate same time period indicates the airplane descended to FL249.
  • The NTSB Performance Study indicates that based on radar returns between 1233:40 and 1234:00, the bank angle increased from 50 degrees to approximately 100 degrees, while the radar data indicates that for the approximate same time frames, the airplane descended from FL249 to FL226. The right descending turn continued and between 1233:59, and 1234:12, the airplane descended from 22,600 to 16,700, and a change to a southerly heading was noted. The NTSB Performance Study indicates that the maximum positive load factor of 4.6 occurred at 1234:08, while the NTSB Electronic Device Factual Report indicates that the maximum recorded airspeed value of 338 knots recorded by the EIS occurred at 1234:14. The next recoded airspeed value 1 second later was noted to be zero. Simultaneous to the zero airspeed a near level altitude of 15,292 feet was noted.
  • Between 1234:22, and 1234:40, the radar data indicated a change in direction to a northeast occurred and the airplane descended from 13,300 to 9,900 feet. The airplane continued generally in a northeasterly direction and between 1234:40 and 1235:40 (last secondary radar return), the airplane descended from 9,900 to 800 feet. The last secondary radar return was located at 27 degrees 49.35 minutes North latitude and 081 degrees 28.6332 minutes West longitude. Plots of the radar targets of the accident site including the final radar targets are depicted in the NTSB Radar Study which is contained in the NTSB public docket.
  • At 1235:27, the controller asked the pilot to report his altitude but there was no reply. The controller enlisted the aid of the flight crew of another airplane to attempt to establish contact with the pilot on the current frequency and also 121.5 MHz. The flight crew attempted on both frequencies but there was no reply.
  • At 1236:30, the pilot of a nearby airplane advised the controller that he was picking up an emergency locator transmitter (ELT) signal. The pilot of that airplane advised the controller at 1237:19, that, "right before we heard that ELT we heard a mayday mayday." The controller inquired whether the pilot had heard the mayday on the current frequency or 121.5MHz, to which he replied that he was not sure because he was monitoring both frequencies. The controller inquired with the flight crews of other airplanes if they heard the mayday call on the frequency and the response was negative, though they did report hearing the ELT on 121.5 MHz. The controller verified with the flight crew's that were monitoring 121.5 MHz whether they heard the mayday call on that frequency and they advised they did not.
  • A witness who was located about 1.5 nautical miles south-southwest from the crash site reported that on the date and time of the accident, he was inside his house and first heard a sound he attributed to a propeller feathering or later described as flutter of a flight control surface. The sound lasted 3 to 4 cycles of a whooshing high to low sound, followed by a sound he described as an energy release. He was clear the sound he heard was not an explosion, but more like mechanical fracture of parts. He ran outside, and first saw the airplane below the clouds (ceiling was estimated to be 10,000 feet). He noted by silhouette that parts of the airplane were missing, but he did not see any parts separate from the airplane during the time he saw it. At that time it was not raining at his location. He went inside his house, and got a digital camera, then ran back outside to his pool deck, and videotaped the descent. He reported the airplane was in a spin but could not recall the direction. The engine sound was consistent the whole time; there was no revving; he reported there was no forward movement.

Source: NTSB ERA12FA385


3

Analysis

  • Examination of the separated structural components revealed no evidence of pre-existing cracks on any of the fracture surfaces. Postaccident examination of the primary flight controls and engine revealed no evidence of preimpact failure or malfunction. The flaps were found in the retracted position, and the landing gear was extended; it is likely that the pilot extended the landing gear during the descent. The horizontal stabilizer trim actuator was positioned in the green arc takeoff range, the impact-damaged aileron trim actuator was in the left-wing-nearly-full-down position, and the rudder trim actuator was full nose right. The as-found positions of the aileron, rudder trim, and landing gear were not the expected positions for cruise climb. Examination of the relays, trim switch, and rudder trim circuit revealed no evidence of preimpact failure or malfunction, and examination of the aileron trim relays and aileron trim circuit revealed no evidence of preimpact failure or malfunction; therefore, the reason for the as-found positions of the rudder and aileron trim could not be determined. Impact-related discrepancies with the autopilot flight computer precluded functional testing. The trim adapter passed all acceptance tests with the exception of the aural alert output, which would not have affected its proper operation. The CAWS log entries indicated no airframe or engine systems warnings or cautions before the airplane departed from controlled flight. A radar performance study indicated that the airplane did not enter an aerodynamic stall, and according to the CAWS log entries, there was no record that the stick pusher activated before the departure from controlled flight.
  • Before purchasing the airplane about 5 weeks earlier, the pilot had not logged any time as pilot-in-command in a turbopropeller-equipped airplane and had not logged any actual instrument flight time in the previous 7 years 4 months. Additionally, his last logged simulated instrument before he purchased the airplane occurred 4 years 7 months earlier. Subsequent to the airplane purchase, he attended ground and simulator-based training that included extra flight sessions in the accident airplane, likely due to his inexperience. The training culminated with the pilot receiving his instrument proficiency check, flight review, and high-altitude endorsements; after the training, he subsequently logged about 14 hours as pilot-in-command of the accident airplane. Although the pilot likely met the minimum qualification standards to act as pilot-in-command by federal aviation regulations, his lack of experience in the make and model airplane was evidenced by the fact that he did not maintain control of the airplane after the autopilot disengaged. The airplane was operating in instrument conditions, but there was only light rime ice reported and no convective activity nearby; the pilot should have been able to control the airplane after the autopilot disengaged in such conditions. Further, his lack of experience was evident in his test of the autopilot system immediately following the airplane's departure from controlled flight rather than rolling the airplane to a wings-level position, regaining altitude; only after establishing coordinated flight should he have attempted to test the autopilot system.

Source: NTSB ERA12FA385


4

Cause

The failure of the pilot to maintain control of the airplane while climbing to cruise altitude in instrument meteorological conditions (IMC) following disconnect of the autopilot. The reason for the autopilot disconnect could not be determined during postaccident testing. Contributing to the accident was the pilot's lack of experience in high-performance, turbo-propeller.

Source: NTSB ERA12FA385

References

(Source material)

Factual Report Aviation, PC-12 N950KA, NTSB ID: ERA12FA385, 06/07/2012, National Transportation Safety Board.